[1]许跃,许洪祝,周启立,等.致密气压裂返排液及生产水处理耦合工程优化[J].中国给水排水,2025,41(6):117-121.
XUYue,XU Hong-zhu,ZHOUQi-li,et al.Optimization of Coupled Tight Gas Fracturing Flowback Fluid and Production Water Treatment Project[J].China Water & Wastewater,2025,41(6):117-121.
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XUYue,XU Hong-zhu,ZHOUQi-li,et al.Optimization of Coupled Tight Gas Fracturing Flowback Fluid and Production Water Treatment Project[J].China Water & Wastewater,2025,41(6):117-121.
致密气压裂返排液及生产水处理耦合工程优化
中国给水排水[ISSN:1000-4062/CN:12-1073/TU]
卷:
第41卷
期数:
2025年第6期
页码:
117-121
栏目:
出版日期:
2025-03-17
- Title:
- Optimization of Coupled Tight Gas Fracturing Flowback Fluid and Production Water Treatment Project
- Keywords:
- tight gas; fracturing flowback fluid; production water; technical transformation; process optimization
- 摘要:
- 临兴中区LX-156水处理站处理规模为480 m3/d,原采用“调节/涡凹气浮/多介质过滤/精细过滤”处理工艺。为满足生产建设要求及解决工艺运行不稳定等问题,该水处理站改造后处理规模提升至1 080 m3/d,根据压裂返排液及生产水水质特点,采用“预处理/一体化破胶/涡凹气浮/高密度斜管沉降/保安过滤/精细过滤”耦合工艺。该工程采用一体化撬装式设备进行原位扩容,在破胶脱稳30 min,气浮处理24 min,高密度斜管沉降器投加PAC 300 mg/L、PAM 15 mg/L、NaOH 800 mg/L的条件下,整个工艺稳定运行128 d,处理达标回注水125 435 m3,出水关键指标含油量≤30 mg/L、悬浮物≤10 mg/L、颗粒直径中值≤4 μm,满足《碎屑岩油藏注水水质推荐指标及分析方法》(SY/T 5329—2012)的高渗透率油层回注水水质标准。
- Abstract:
- The LX-156 water treatment station in Linxing Central District with treatment capacity of 480 m3/d, originally adopted the treatment process of conditioning/turbulent air flotation/multi-media filtration/fine filtration. To satisfy the production construction requirements and solve the process instability problem, the capacity of the water treatment station was increased to 1 080 m3/d after renovation. According to the characteristics of fracturing flowback fluid and production water quality, the coupled process of pretreatment/integrated rubber breaker/vortex concave air flotation/high-density sedimentation/security filtration/fine filtration was adopted. In?situ capacity is expanded using integrated skid-mounted equipment. By breaking and destabilizing for 30 min, air flotation treatment for 24 min, as well as adding PAC of 300 mg/L, PAM of 15 mg/L, and NaOH of 800 mg/L in high density sedimentation, 125 435 m3 of refill water was treated up to the standard after operated stably for 128 days. The key effluent indexes include oil content ≤30 mg/L, suspended solids concentration ≤10 mg/L, and diameter median of suspended solids ≤4 μm, which met the water quality standards for reinjection water from high permeability oil reservoirs in Water Quality Standard and Practice for Analysis of Oilfield Injecting Waters in Clastic Reservoirs (SY/T 5329-2012).
更新日期/Last Update:
2025-03-17