[1]杨墨,刘毛,邓涛,等.混凝—气浮—过滤深度处理A2O工艺二沉池出水[J].中国给水排水,2020,36(19):89-94.
YANG Mo,LIU Mao,DENG Tao,et al.Advanced Treatment of Effluent from Secondary Sedimentation Tank of A2O Process by Coagulation–Dissolved Air Flotation–Filtration[J].China Water & Wastewater,2020,36(19):89-94.
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YANG Mo,LIU Mao,DENG Tao,et al.Advanced Treatment of Effluent from Secondary Sedimentation Tank of A2O Process by Coagulation–Dissolved Air Flotation–Filtration[J].China Water & Wastewater,2020,36(19):89-94.
混凝—气浮—过滤深度处理A2O工艺二沉池出水
中国给水排水[ISSN:1000-4062/CN:12-1073/TU]
卷:
第36卷
期数:
2020年第19期
页码:
89-94
栏目:
出版日期:
2020-10-01
- Title:
- Advanced Treatment of Effluent from Secondary Sedimentation Tank of A2O Process by Coagulation–Dissolved Air Flotation–Filtration
- Keywords:
- effluent from secondary sedimentation tank; A2O process; advanced treatment; coagulation; dissolved air flotation; filtration; recycling ratio; coagulant dosage
- 摘要:
- 以武汉市某污水处理厂A2O工艺二沉池出水为原水,进行了混凝—气浮—过滤深度处理工艺中试研究。结果表明:①在表面负荷为8~12 m3/(m2·h)条件下,该深度处理工艺出水COD为17 mg/L、浊度<0.5 NTU、TP<0.1 mg/L;②表面负荷对出水水质的影响不大,当分流比为15%、混凝剂(聚合硫酸铝铁)投加量为10 mg/L时,处理效果最优,对浊度、COD、TP的去除率分别为94%、63%和90%;③当分流比较小(10%)时,增加混凝剂用量可以降低出水浊度与COD,当分流比较大(20%)时,混凝剂用量不再是限制因素,对出水浊度和COD影响不大;④混凝—气浮工艺可去除大部分悬浮物、COD和TP,保证了更好的过滤效果与较长的过滤周期。混凝—气浮—过滤工艺的处理效果优于污水处理厂既有高密度沉淀池+精密过滤器深度处理工艺。
- Abstract:
- A pilot study on advanced treatment process of coagulation-dissolved air flotation (DAF)-filtration was carried out in a wastewater treatment plant in Wuhan,and its influent was secondary sedimentation tank effluent of an A2O process. When surface load was 8-12 m3/(m2·h), COD in the effluent of the advanced process was 17 mg/L, turbidity and TP in the effluent of the advanced process were less than 0.5 NTU and 0.1 mg/L. Surface load had little effect on effluent quality. The optimum operational condition was obtained when the recycling ratio was 15% and the dosage of coagulant (polymeric aluminum ferric sulfate) was 10 mg/L, and removal rates of turbidity, COD and TP were 94%, 63% and 90%, respectively. When recycling ratio was relatively small (10%), increasing coagulant dosage could reduce turbidity and COD in the effluent. When recycling ratio was large (20%), the coagulant dosage was no longer a limiting factor, and it had little impact on turbidity and COD in the effluent. In this process, coagulation-DAF process removed most of the suspended solids, turbidity and COD, in which good filtration efficiency and longer filtration cycle were obtained. This process achieved better treatment efficiency than the existing advanced treatment process of high-density sedimentation tank and precision filter.
相似文献/References:
[1]高海英,邓磊,侯晓庆,等.MBR工艺在西安经开草滩污水处理厂中的应用[J].中国给水排水,2020,36(8):63.
[2]李玉宾,李树华.百乐克池不停水升级改造为A2O生化池工程设计[J].中国给水排水,2020,36(20):129.
LI Yu-bin,LI Shu-hua.A Renovation Design Case of the A2O Biochemical Tank Transformed from BIOLAK Tank without Water Interruption[J].China Water & Wastewater,2020,36(19):129.
更新日期/Last Update:
2020-10-01